Engine
I was a
little indecisive about what part of the car to tackle next. The chassis and running gear is almost
complete, so I decided to work on the engine alongside it as I’m waiting for
some parts to complete the brakes and steering.
The engine/gearbox is an enormous and extremely heavy unit, far too
heavy to manhandle around the garage. So
much so, in fact, that I needed to build a custom dolly to enable me to work on
it without the risk of falling over and causing damage to itself or me! So, this is where I’m at currently.
When I bought the car, I did consider attempting to start the engine after
performing some basic maintenance work.
Given that it’s not run for probably 30 years, I decided maybe that
wouldn’t be the wisest decision, as the oilways could be blocked or any number
of other issues which could cause the engine to self-destruct. So, I intend to partially strip it down
initially, and make an assessment based on what I find then. The crank rotates freely and it feels nice
and snug, but it’s obviously impossible to really know what’s going on in there
until it’s taken apart. I’ll be wheeling
it outside to clean it up first. Then it
will be off with the carbs and ancillaries before taking off the heads and
revealing the bits that will decide whether it’s a simple rebuild or if it will
require a re-bore and new oversized pistons, along with the cost that’s
associated with it. Fingers crossed!
OK, the car
is now a rolling shell at least, with the steering complete and just the brake
calipers required to finish it off. I’m
holding out on those as they need either new sleeves fitted, which I am unable
to find anyone to do at the moment, or to replace with new units which is
mighty expensive. There’s no rush for
them, so I’ve put them on the back-burner for now. So, with a line drawn under
the rolling shell, the next on the list is to tackle the engine.
I stripped
off all of the ancillary items without too much trouble, ensuring I took plenty
of photos of each component and carefully labelling everything in readiness for
its reassembly.
The rocker chamber looked in good shape, but the next step would dictate my
workload (and expenditure!) for the next year, so it was with great
apprehension I undid the head bolts and started to remove the first cylinder
head. It came away surprising easy and didn’t require any ‘persuasion’ at
all.
Firstly I inspected the bores. These
four are perfect, even the piston ring threshold was barely visible, and I
couldn’t feel it at all with the fingernail test. Great news indeed.
The next thing to look at was the cylinder head. These are made of aluminium and if the car
hasn’t been well maintained, and has been topped up with straight water instead
of the correct coolant, then the channels erode badly and this can creep into
the combustion area. This is very bad
news indeed, as can make them totally unusable.
Well, the last owner had obviously been conscientious with the servicing
because the corrosion in the head was minimal.
A BIG sigh of relief. I had to end my work there for the day, and will
tackle the offside head tomorrow, but from what I saw with the nearside head
today, I am hopeful that it will be of a similar condition. I drove home tonight with a big smile on my
face. A good day, a very good day!
So tonight I removed the second head and was pleased to find that this too,
along with the pistons/bores, was also in great condition.
I carried on and removed more of the engine components until I praised off the
tappet chest cover to expose the camshaft and followers. Hmmm, not so good there. The camshaft has a few lobes that have
suffered some corrosion. Not the end of the world, and far better than the
bores/heads needing work, but not ideal.
Fortunately the cam followers have not been
damaged at all, so will be re-used. At
least it’s just a case of buying a replacement/used item and fitting it, no
engineering work required. Corrosion
damage like this is caused by condensation in the engine, usually from short
trips, but because it’s so severe in this case, I think it is more likely to
have been because the engine has been laid up for so many years.
So, a new (or rather ‘different’) camshaft is on order and it’s time to check
out the crankshaft and big end bearing shells.
The crank journals were perfect, both for the main bearings and the big
ends. Very happy about that indeed. Next
to check the actual bearing shells.
They were (almost) all perfect too. All
of the big ends and most of the mains were good (above), but the centre main
bearing shells (below) show a little bit of wear. So out of thirteen pairs,
just one pair showed wear, and even that was only just a little bit of the
copper breaking through at the edges. There were no scratches, groves or damage
at all. All three pairs of centre main bearings have a reputation for being the
first to suffer in a worn engine, but I appear to have escaped lightly which
gives me some confidence that it hasn’t done too many miles. I’ll replace all of the shells now as a
matter-of-course, but they certainly would have held out for quite a while
yet. The effort involved to remove and
strip the engine, it would be foolhardy not to use this opportunity to replace
them with new.
Time to give
the engine block a clean-up. I had
already checked for damage and there is none.
The water jacket was however, very murky inside. The rust had built up on the internal
casting, and needed a good cleaning. It
wasn’t so bad to cause any blockages, but it will certainly help with cooling
now that the water can travel unimpeded around the cylinders. I used a length of 6mm steel wire to push
around the insides where a screwdriver wouldn’t reach. It’s ideal to use as it frays in use and acts
like a chimney sweeps brush. Eventually
it gets too frayed, but you just chop off a few inches and start again. I also
popped out all of the core plugs to give myself better access to the water
jacket, and it’s wise to change them while the access is good anyway.
The resultant gloop spilled out of the lower core plug hole. Nice…… I guess it will take a few water flushes to
remove the remaining residue from the system, but I’ll wait until it’s back together and the system is sealed to do that,
before filling with the correct coolant mixture to prevent any reoccurrence.
Before I can start on the reassembly, the final job is to clean the
pistons. It’s a rewarding job to see the
transformation as you remove the years of carbon build up and the bright alloy
reappears. Well, it’s rewarding the
first time, the downside of it being a V8 is that there are a further seven to
go…
The piston rings were all pretty good, just one had gummed up and needed a
little bit effort to remove. I checked
each ring in the bore, and they were all just a smidge outside the tolerance of
0.009 to 0.014 inches. Most were about
2-3 thou over that, with the gummed up one a bit worse at 0.021 inches. I’ll measure the bores later but I’m hopeful
that it’s the rings that have worn as there doesn’t appear to be any lip in the
sleeve at all. Everything on the engine
so far has been standard sizing, so it’s never had a cylinder rebore or a
crankshaft regrind.
Well, things
were going well with the strip-down. Too
well. I guess I was pushing my luck too
far to expect that the camshaft would be all that was damaged. I removed the heads and they looked ok upon
initial inspection. The main area that
these alloy heads suffer damage is around the water channels. They corrode due to lack of, insufficient or
incorrect antifreeze being used. This
becomes a problem when it extends past the perimeter of the head gasket seal,
and in severe cases can even breach the wall into the combustion chamber. This was obviously the first thing I
checked. Both heads are fine in this
regard, so I was at that point very pleased.
The top of
the first head also looked to be problem free with no slack in the valve guides
after removing the springs.
This is where I lucked out! The OS head also has intact water channels, but
upon turning over to clean the rocker chamber I was faced with two cracks in
the alloy. Arrrrrggghhhhh!
That’s put a massive spanner in the works. This damage is above the water
jacket in the head and is caused by the water turning to ice and expanding in
the cavity. With nowhere to go,
something has to give, and in this case it was the alloy head. So now I am
faced with one of two options. One, buy
a replacement head or two, get this one repaired. I have seen repairs made to these heads, and
it seems a reasonably common failure point. Here are two that have been done
that I found online.
I’ve made some enquires and I can find a replacement head, but it’s not
cheap. I’ve emailed a few places for a
repair quote but no reply yet. I’m still
waiting for the main bearing shells and piston rings to come back in stock, so
I’ll crack on with cleaning and preparing the other engine components. First up is the sump. I was not looking forward to this, and it
took two days. The outside was covered in rock hard, oil coated mud and the
inside floor was full of congealed oil, which had the consistency of yoghurt.
What a messy job. I don’t have any
‘before’ images, but it looks in reasonable shape now.
I had a reply from a local engineering firm to say that they would take a look
at my head as they were quite confident that they could weld it for me. Within 24hrs the head was back with me and I
was heading home having paid what I consider a reasonable fee for the
privilege. They had to chase the crack
a little as they welded, and this meant that there’s a little excess metal in
the pushrod tube. These are oversized,
but I may need to trim a little away to get the end of the pushrod through. I
will have to wait and see.
In the meantime, the bearings and rings have arrived, so I can start on the
rebuild soon. Before that though,
everything needs cleaning. The
crankshaft of the V8 is unusual because in each big-end cavity, there is a
sludge trap where any particles in the oil are collected due to the centrifugal
force when the engine is running.
Sometimes there are spoonfuls of the
stuff! To gain entry to these, there are
four plugs which need to be removed.
They are renowned to be a PITA to remove as the threads are peened over
in the factory to prevent them coming loose.
In an attempt to avoid taking them out, I instead flushed the oilways
with copious amounts of WD40 and used a flexible cable to dislodge and dissolve
any sludge. But in the end I decided
that I wouldn’t be confident that a stray piece would block the oil feed to the
bearings with disastrous consequences.
So, I used a Dremmel drill to remove the burr from peening and they came
out reasonably easily, with just one suffering a little bruising of the hex
socket from the allen key. I had been wise to be so
thorough as there were still a couple of little bits of clay remaining, hardly
anything but at least I can rest easy knowing they are now absolutely clean.
I wanted to ensure that the threads were perfect and that the plugs did not
create any swarf when they were reinserted, so I ran a plug tap down the thread
to clean them up and clear any remaining debris.
Some more cleaning and polishing done on some of the remaining components. I actually did a better job than this on the
valves, but this was a capture half way through. I’ll post some completed ones
when they’re back in the head.
The valve train (rockers) all ready to go. Interestingly some are steel and
some bronze, or at least that’s the colour of them. All have hardened tips for the valve contact
areas though, which did need a little polishing to remove the wear marks.
I was looking
forward to polishing the rocker covers, because polished alloy can look so
good. My enthusiasm soon subsided though
when I remembered just how hard it is.
Here are a couple of before/after split shots. I think the effort was worthwhile, now that
my arms have recovered.
I won’t be needing any of the above polished ancillaries for some time, but I think
I turned to these frivolous items because I am quite nervous of starting the
re-assembly of the engine. These engines
are not easy to come by, and the costs involved in rectifying any serious
mistakes could push back the restoration by years. So I am fully aware of the
importance of getting things right, first time. We are not at home to Mr
Cock-Up.
I forgot to
take photos of the shells and crank prior to assembly, due to the pressure I
think. Anyhow, it went in quite well and
I used some assembly lube along the way to ensure the bearings are not running
dry on the first start-up. The only
issue was when I fitted the rear cap which is incorporated into the oil
pump. Back in the day, instead of a
rubber oil seal on the crankshaft, most cars used a rope (yes, that’s right….a
rope!) that fitted in a groove in the block and cap to prevent oil loss. This
is supplied in its raw state, and needs to be fitted and compressed to the
correct size before fitting the crank.
Well, I didn’t have the correct part, and so instead used the crank
itself to act as a sizing tool. It was
initially very tight indeed, but after an overnight settling in period and
removal of the very thick lube (I used a thin oil instead) it became far easier
to rotate. I’m happy with it now but
would have been uncomfortable leaving it so tight that it could mask any other
issues. I have heard of people using two
batteries in parallel to start the engine for the first time due to a tight
rope seal!
So with the crank in and torqued down, time to insert the pistons.
The original pistons were re-used as the bores were not worn, but it would seem
churlish not to go to all of this effort and not replace the rings.
Here piston number 1 is being fitted using a piston ring compressor to ease it
into the freshly honed bores. The new
compression rings do have some manufacturing tolerance and I had to try a
couple before finding the best fit, no problem with the oil control rings, they
are a loose fit anyway. The compression rings though, are tending to be a bit
long (tight) but the instructions state that the ends should not be filed to
fit. I’m unsure what I’ll do if the last
couple don’t match the bores. I’ll cross
that bridge when I get to it.
So here they are, all pistons in and all rings fitting within tolerance. With
no option other than to file the ends to fit, I filed the ends to fit. I can’t
see I had much option really. ‘Gapping
the rings’ by filing the ends is how they’ve been done for decades, so not sure
why my rings said not to on the pack.
Anyhow, they’re in now.
With everything now torqued down and all tab washers bent over, it was time to
put the sump on. There is no gasket on
the flat areas, just a rubber tube at each ends for the semi-circular seal. These were a right pain as they appear to be
too large in diameter and there seems to be too much rubber to squash
down. I did it in the end, but was quite
difficult.
Next I fitted a new worm gear for the oil pump and distributor (well, it wasn’t
brand new, but almost!) Mine had worn a bit as the gear is made from brass
against the cast of the camshaft. Here’s
the difference.
There would have been a fair bit of play, but as the shaft is only ever driven,
it doesn’t matter too much. More
importantly though is that the ends of the teeth can get very thin and
eventually break off. Compare the
thickness of the two above.
I then fitted the shaft with the new gear into the block and down into the oil
pump. Hmmm, something wasn’t right. It was free 90% of the way down, then the
last bit tightened quite a bit. I didn’t
know if this was normal and neither the manual nor the internet gave any
clues. No option but to remove the sump,
the one that I just had so much trouble getting on! When it was removed, I could see that the
shaft of the drive was not quite central on the input tube of the oil
pump. The pump sits on the block and is
fastened by three bolts. There is no adjustment
to be made, so I wasn’t sure how to go about centralising the two. Fortunately, the tolerances at Daimler back
in the day were not as good as now, and after slackening the bolts I was able
to tap the body of the oil pump gently around with a hammer which gave me the
fine adjustment I needed. Everything is
now smooth as silk and I’m much happier and glad I decided to investigate.
So with the sump back on, it was time to fit the camshaft. I bought a replacement as mine was too badly
corroded to use. The one I bought was
much better, but not like new. The lobes
and journals both have a very slight amount of pitting, although for a 55 year
old car, I think I’m just being fussy.
So I phoned for a price for a new one, £850. Suddenly the pitting didn’t seem so bad after
all.
I coated the journals with assembly lube and popped it in along with aligning
the worm gear for the oil pump and reattaching the timing chain/sprockets. These were perfectly usable and showed no
real signs of wear. I had taken
photographs of the timing marks and sprocket positions before disassembly to
ensure that they were reassembled correctly.
The consequences of getting this wrong could be disastrous.
After fitting
the tappet chest cover, the heads were the next to be fitted. They were true and flat, which I was pleased
about, and only required a smooth over with 600grit to make sure they would
mate well with the gasket. I had already
assembled them and lapped in the valves.
It’s been a while since I’d lapped valves and I’d forgotten what a pain
the arse it is, especially with 16 to do.
Some of the valve seats had a small amount of pitting which needed them
to be recut, but only by a very small margin and it only took a couple of turns
of the tool to be deep enough to make them like new. A last check that there was no debris remaining
and a blow out with the airline, and on they went.
I made the
job of adjusting the tappets a whole lot harder for myself because I’d
pre-fitted the sparkplug tubes on the bench.
This restricted the access to the locking nuts on the inlets. In hindsight it would have been far easier to
adjust the tappets before fitting the tubes, but it wasn’t worth the effort of
breaking the new seals and sealant just to do this. So, I struggled through. The head bolts are not the stretch variety,
so I was able to re-use the old ones.
Another advantage of non-stretch bolts is that they don’t require
re-torqueing after 500 miles, which will save a whole lot of work removing the
rocker covers again.
The duplex chain here was replaced before refitting the tensioner and cover.
The old one, despite not having stretched out of tolerance, but it did have
some corrosion so it was replaced to avoid rapid wear to the chain wheels.
The inlet manifolds are alloy, which always (well, almost always) comes out
well after a clean-up. I wire wheeled
most of the crud off, and media blasted the remaining inaccessible areas. I
will of course, thoroughly clean before fitting to ensure no media remains in
any of the cavities, which would be catastrophic if ingested by the engine.
The first of the ancillary items to be tackled were the carburettors. They were dirty but after a quick clean in
the ultrasonic cleaner, they came out quite well. I was a little sceptical about using the
parts washer, but I was surprised how effective it was. Very contaminated parts still require a
little brush after cleaning, or even a second dip in the bath. They are reasonably priced on the internet
and a worthwhile purchase if you have lots of work for it to do. It cleans the internal, inaccessible areas
too, which is quite important for items such as carbs.
These are the HD6 version of SU carbs, and the D denotes they are diaphragm
carbs. There is a small rubber disk in
the bottom which moves vertically when the choke is applied. Because the car had been standing for so
long, these rubber parts have become very hard and inflexible. They are not extortionate to replace, but not
cheap either. After a search online, I
discovered a way to rejuvenate the rubber is to soak in a bath of DOT3 brake
fluid. At less than a tenth of the price
of new diaphragms, it’s worth a shot. It takes 3 – 4 days to penetrate the
rubber, and they are currently soaking away.
The rest of the carbs have been assembled loosely so that I can progress
with the rest of the setting up of the linkages etc.
Before I finally fit the carbs, there is a water pipe connection to the
manifold, which is almost impossible (with my gnarly old hands at least!) to
fit afterwards. So I’ll get that on,
along with the rest of the pipework so I can run the engine wet. This means that I confirm that it is leak
free before refitting into the car. The
old pipework was made up of a combination of rubber connectors and metal pipe
sections. These inevitably rust to
nothing, so I will be replacing much of the waterways with copper plumbing
pipework instead. It’s a common
upgrade/modification and far cheaper than genuine Jaguar replacements. So that’s next……
So I’m at the
point where everything (except the distributor) is back on the engine. I’ve refitted the dynamo bracket after
deciding not to upgrade to an alternator.
The bracket to convert is almost a £100 on its own, and I found a
cheaper alternative. It’s a Dynamator, a cross between a dynamo and alternator. Yeah, I know it sounds like a made-up name,
but it’s a genuine thing. It looks
identical to the old dynamo, but the insides are replaced with more modern
components. This is good for two
reasons. Firstly as it looks original,
so it keeps the purists happy. Not
really an issue for me though, but what is good for me, is that it utilises the
same old mounting bracket. I’ll also be converting the car to Negative earth,
so I can fit modern electrical components and hi-fi.
Anyhow,
everything is back on and the first test was to crank the engine over. Not to attempt to start it, but just to see
if the engine was loose enough for the aging starter to cope with and also to
confirm the oil pressure was ok with no leaks.
I had already primed the oilways and filled the oil filter bowl by
filling them via the output hole for the oil pressure gauge. It’s a small hole and not designed for
passing a lot of fluid, so it took a while.
I refitted the oil gauge and connected some sturdy cables to an old
battery that I had kept when replacing it from my daily car. It’s not 100%, but good enough for this test
and I’d charged it overnight. I removed
the spark plugs so that the compression wouldn’t make turning it over even
harder. I held the cable on the battery
terminals and the starter motor did its thing.
The cranking speed wasn’t fast, but after a few moments the oil pressure
gauge started to rise. It managed to get
to 25 psi before the battery finally gave out.
Given the slow speed it was turning at the end, I think that’s
fine.
I want to run
the engine on the dolly as I’ve mentioned before, but so I don’t annoy the
neighbours, I need to fit a pair of silencers.
I had one, but needed to get another.
Fortunately, my local National Tyre branch had one in their scrap
skip. They were more than happy to give
it to me, but I felt a right pikey asking for it! Embarrassment over, I headed home to weld
them both on.
Yes, not pretty, but they are only temporary.
The gearbox is also temporary. I
only refitted it to make it the engine more stable when I try to run it. Next job is to finish the distributor and
then it’s the big moment that I’ve been excited for and dreading in equal
measures …….….
THE BIG DAY!
So, I
completed the distributor. It does still
need some work, but not essential to its operation. There’s a spring-steel arm with a felt pad on
the end that lubricates the cam, but I broke it. I tried a replacement spring from a spare set
of points, but I couldn’t drill a hole in it easily. So, with the excitement of actually starting
the engine, I didn’t bother to fit that part and continued with the important
stuff. The points were adjusted to the
handbook specification, but I needed to cut my 0.015” feeler gauge in half as
it was too wide to fit in the aperture of the points. So, yet another tool
‘modified’ for a specific job. I
refitted the distributor and hooked up the HT leads, ensuring they were in the
correct sequence. Nothing left I could
use as an excuse to put off the inevitable any longer. With my spare battery ably assisted with the
good one on my car, I cranked her over until the oil pressure rose. Then, it was out with the fuel and a can of
‘Easy Start’. After about 20 seconds of cranking, whilst simultaneously
rotating the distributor to find the correct timing, she sparked and
stalled. A further couple of cranks and
she was at last running. I had to use
the throttle arm and choke to keep her running at that point, but I was soon
able to use just the throttle. The
funnel of fuel soon ran out and I adjusted the ‘slow running screws’ to
increase the tickover in readiness for the next
start. A quick on-the-fly adjustment and
she was soon ticking over slowly and smoothly and was soon at operating
temperature. To say I was jubilant (and
bloody relieved!) would be more than putting it mildly. I’ll still need to tune her properly, but for
now the aim of the exercise was complete, although I did run a few more funnels
of fuel through because I was so excited.
Plus I wanted to get a good video of her running. (No video? It didn’t happen, yeah?) I did try to embed the video, but MS Word is
having none of it, so if you want to see the engine running, you’ll have to
click the image below -
So, that’s
probably enough excitement for the weekend, and the next job is to remove the
gearbox again and start the rebuild of that.
It’s a Borg Warner BW35 Auto gearbox and I’ll be armed only with the
Daimler manual and what I’ve read on the internet. What could possibly go
wrong!